Author
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Topic: Apollo 13 explosion, but on Apollo 8
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Sceptic1 Member Posts: 23 From: United Kingdom Registered: Feb 2010
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posted 03-28-2011 12:15 PM
How vital was the lunar module, not carried on Apollo 8, to the survival of the astronauts of Apollo 13?It is my understanding that, without the LM's descent engine to make the necessary course alterations, Apollo 13 would simply have coasted on past the moon, with no hope of saving the astronauts. |
SpaceAholic Member Posts: 4936 From: Sierra Vista, Arizona Registered: Nov 1999
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posted 03-28-2011 12:27 PM
Apollo 8 (as well as Apollo 10 and Apollo 11) were injected into free return trajectories and did not require a subsequent burn to return home. |
Nigel Mc Member Posts: 182 From: Sheffield, UK Registered: Jan 2011
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posted 03-28-2011 12:48 PM
The LM oxygen supply was very important to Apollo 13.
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Skylon Member Posts: 309 From: Registered: Sep 2010
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posted 03-28-2011 04:00 PM
quote: Originally posted by Sceptic1: How vital was the lunar module...
It was THE key to the Apollo 13 crew's survival. As noted, Apollo 8 was on a free return trajectory, but for Apollo 13 they needed it to make vital course corrections.However, the Apollo 13 LM also supplied the crew's oxygen and water after the accident. All the CSM had left by the time they powered down was the re-entry batteries. The CSM was dead. If the Apollo 13 accident happened to a CSM flying solo to or from the moon (or in lunar orbit) I can't fathom what could have been done to save the crew. |
SpaceAholic Member Posts: 4936 From: Sierra Vista, Arizona Registered: Nov 1999
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posted 03-28-2011 06:01 PM
More problematic for Apollo 13 and flights prior; post Apollo 13 CSM's had supplemental LH2/LOX in Bay 1 and an auxiliary 400 Amp hour LM battery (in Bay 4 paralleled with Fuel Cell 2), which could be brought online. The decision to not use the SPS was elective and would have been attempted if the LM was not available. |
Skylon Member Posts: 309 From: Registered: Sep 2010
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posted 03-28-2011 10:08 PM
In regards to the direct abort option with the SPS, that was a dicey scenario. Certainly if such an accident happened on Apollo 8, there would be no other choice. But I'm not sure the CSM would have the consumables to limp home. Remember, the direct abort option on Apollo 13 was not exercised, not only because there was worry of damage to the SPS, but because a direct abort meant ditching the LM. Holding onto the LM gave everyone more options for getting the crew home. |
Grounded! Member Posts: 462 From: Bennington, Vermont, USA Registered: Feb 2011
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posted 03-29-2011 06:27 AM
Apollo 8 would have been forced to use the CSM engine and if that had failed, they certainly would have perished. |
mooncollector Member Posts: 104 From: Alabama, USA Registered: Feb 2011
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posted 04-03-2011 09:33 PM
What if the explosion was on Apollo 10?Snoopy was not loaded with consumables enough for a lunar landing. It was basically only prepared to handle about 10 hours +/- of independent flight in lunar orbit, and if I recall correctly the descent stage didn't even come close to being fully fueled. I don't think Snoopy could have done the job that Aquarius did. |
SpaceAholic Member Posts: 4936 From: Sierra Vista, Arizona Registered: Nov 1999
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posted 04-03-2011 11:43 PM
Snoopy and Aquarius descent stage carried almost identical propellant loads (about 18,000 pounds) thus the Apollo 10 LM was capable of performing the same burn. It was the ascent stage propellant loadout that differed (by about 50 percent). |
Tykeanaut Member Posts: 2222 From: Worcestershire, England, UK. Registered: Apr 2008
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posted 04-07-2011 06:14 AM
I hadn't really thought of this scenario on Apollo 8 until Richard Gordon mentioned it during his recent talk in Yorkshire, UK. Apollo 8 truly was a bold step when you consider what could have happened. |
mooncollector Member Posts: 104 From: Alabama, USA Registered: Feb 2011
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posted 04-21-2011 11:30 AM
quote: Originally posted by SpaceAholic: Snoopy and Aquarius descent stage carried almost identical propellant loads...
That means that a DPS direct abort was possible, but would Snoopy have been able to sustain the three men for the +/- 24 hours it would have taken for the return to Earth from the point they were at in the flight? Everything I have heard indicates that the consumables (O2, water, etc.) on board Snoopy would only have lasted for about 10 hours for a two-man crew. Assuming, as on Apollo 13, they had nothing to work with at all from the SM. I'm glad we never had to find out. |
SpaceAholic Member Posts: 4936 From: Sierra Vista, Arizona Registered: Nov 1999
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posted 04-21-2011 12:08 PM
Available consumables (with the previously mentioned exception of ascent stage propellant) were almost identical on both LMs; in fact at jettision, only half the on board O2 was expended in Aquarius's descent stage and none utilized from the ascent stage; 50 pounds water (of the 330 pounds uploaded) remained. |
Scottvirgil Member Posts: 12 From: London UK Registered: Aug 2019
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posted 09-15-2021 05:31 AM
I was just thinking about some whatiffery and imagining the following Apollo conversation. 555520 CDR I believe we've had a problem here.555529 CAPCOM This is Houston. Say again, please. 555535 CDR Houston, we've had a problem. We've had a MAIN B BUS UNDERVOLT. CAPCOM OK 8, we're looking at it. So, the question is, what would have happened if this had been Apollo 8 rather than Apollo 13. The general opinion is that this would be unsurvivable, but presumably some action would be taken by Houston and by the crew.What might they try to do? Do they throw caution to the wind and blast the SPS immediately and desperately try something whilst homeward bound? Or do they just accept the crew is lost? Do the crew suffocate, or freeze to death, or throw open the hatch and end it quickly? Editor's note: Threads merged. |
David C Member Posts: 1299 From: Lausanne Registered: Apr 2012
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posted 09-15-2021 06:19 AM
No-one would just sit there and die without trying something. In my opinion, they would have tried burning the SPS for an immediate turn around and come home as soon as possible. My feeling would be that if it ignited, and if it didn't immediately blow up, then there would be a chance of getting a full burn. Of course they'd probably still not have made it, but you have to give it your best shot. |
Jim Behling Member Posts: 1683 From: Cape Canaveral, FL Registered: Mar 2010
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posted 09-15-2021 07:46 AM
Firing the SPS would do no good. In all cases, the crew would be dead within 4 to 5 hours after the explosion. No oxygen other than what was in the cabin. No power for communications after the CM batteries die. No lights or instruments. No attitude control. No heat. No power for fans to circulate air through LiOH cartridges. |
garymilgrom Member Posts: 2062 From: Atlanta, GA Registered: Feb 2007
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posted 09-15-2021 08:16 AM
With all due respect I see no value in these types of conjecture. What if John Glenn burned up on re-entry? What if Wally Schirra fired the ejection seats? What if Neil Armstrong and Dave Scott died on Gemini VIII? What if the N-1 worked perfectly? What if foam didn't come off the ET? All of these events are in the past and they didn't happen so what's the point of speculating? |
randy Member Posts: 2488 From: West Jordan, Utah USA Registered: Dec 1999
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posted 09-15-2021 08:44 AM
I agree with Gary. Why speculate about this? What good does it do? |
Robert Pearlman Editor Posts: 47142 From: Houston, TX Registered: Nov 1999
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posted 09-15-2021 08:48 AM
"What if" questions can be a way to learn more about a particular topic by taking a look at it from a different perspective. In this case, about the Apollo 13 explosion, it is really a discussion about the capabilities of the command and service modules, as well as what state the Apollo 13 spacecraft was by the time the crew returned to Earth. Not all "what if" questions are useful, but some can result in a good discussion. |
Space Cadet Carl Member Posts: 271 From: Lake Orion, MI Registered: Feb 2006
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posted 09-16-2021 10:38 AM
Not all would agree, but Apollo 8 was just about as gutsy and dramatic as Apollo 11 to me. Witnessing that Christmas Eve broadcast while laying underneath our Christmas tree was huge. |
holcombeyates Member Posts: 286 From: UK Registered: Dec 2010
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posted 09-16-2021 11:48 AM
I read somewhere that the Apollo 13 oxygen tank was scheduled to be used on an earlier mission. Had that happened with a LM in tow it would have probably been ok, but might have postponed the first moon landing and potentially missed Kennedy’s goal. |
randy Member Posts: 2488 From: West Jordan, Utah USA Registered: Dec 1999
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posted 09-16-2021 01:46 PM
If memory serves, that earlier mission was Apollo 10. |
schnappsicle Member Posts: 404 From: Houston, TX, USA Registered: Jan 2012
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posted 10-04-2021 12:36 PM
You are correct. The tank that ruptured on Apollo 13 was originally installed in the Apollo 10 SM. The oxygen tank was removed from Apollo 10 to fix a potential electromagnetic interference problem and replaced with another one.Had it stayed on Apollo 10, it would have most likely delayed Kennedy's stated challenge. The death of Sergei Korolev in 1966 greatly diminished any chances the Soviet Union had of landing men on the moon before the United States. So while we still would have been first, there's a good chance it wouldn't have happened as quickly as it did. |
pterodactyl Member Posts: 23 From: Registered: Feb 2006
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posted 10-04-2021 03:38 PM
Years ago I made the comment to a member of the Apollo 8 crew that "it was a good thing you didn't have an Apollo 13 type failure". The reply was quick and unequivocal, "Apollo 8 would NOT have had that failure." The implication was that the Apollo 8 crew would have monitored the instrumentation voltmeter and seen the short circuit when the heater switch was actuated. The heater would have then been turned off and the explosion averted. |
Paul78zephyr Member Posts: 732 From: Hudson, MA Registered: Jul 2005
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posted 10-04-2021 04:51 PM
quote: Originally posted by schnappsicle: Had it stayed on Apollo 10...
...the failure of O2 tank 2 may never have happened at all. The problem was not simply that the O2 tanks had been built with inadequately rated thermostats, but that the tank (as part of the complete "oxygen shelf") had been subject to a mechanical shock when it was inadvertently dropped during its removal from SM-106. It was hypothesized by the Apollo 13 Review Board that this shock loosened an internal joint in the fill/drain tube (or exacerbated an already ill fitting joint) on that tank which subsequently prevented the tank from being drained after the CDDT using the "normal" de-tanking procedure. This led to the (somewhat ill thought out) "special" de-tanking procedure that relied on the thermostats, which were inadequate, etc, etc, etc. Had the tank never been removed — or at least not dropped — there is a possibility that the fill tube would not have been loosened, that the tank would have de-tanked normally after the CDDT, etc, etc, etc, and the accident never occurred. Keep in mind that the O2 tanks with the inadequate thermostats flew - without issue - on six manned missions prior to Apollo 13. |
Andy Anderson Member Posts: 100 From: Perth, Australia Registered: Dec 2009
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posted 10-04-2021 10:17 PM
quote: Originally posted by pterodactyl; The reply was quick and unequivocal, "Apollo 8 would NOT have had that failure."
I wonder what was said that implied the Apollo 8 crew would have been closely monitoring the "voltmeter" during a cryo stir or how they believed the cryo stir should have been carried out. (I assume that of the three crew members, Jim Lovell did not make the comment)For a start there is no checklist procedure that required the crew to monitor the AC Volts gauge reading (which is way down on the lower right of Panel 3) during a cryo stir and also, even if it had been monitored, it would have required in the case of Apollo 13, the associated monitor switch to be positioned to one of the available phase selections for AC Bus 2 (not AC Bus 1). The normal EPS System Check checklist states:
- H2 PRESS (2) - 225-260 psia
- O2 PRESS (2) - 865 - 935 psia
- SURGE TK PRESS -865-935 psia
- H2 QTY (2) - record
- O2 QTY (2) - record
- CRYO FANS - OF; ON as req'd
The switches for the O2 tank fans are on the upper right of Panel 2 and at the time, Jack Swigert was in the left hand seat for this additional cryo stir partly occasioned by the earlier O2 tank quantity gauge failure.The following information was sourced from the "Report Of The Apollo 13 Review Board - Appendix B" and "Part 4." of the "Final Report." The activation of the fans in O2 Tank 2 at 55:53:20 initially produced indications of a fuel cell current increase of 1 ½ amperes and a drop in AC Bus 2 volts of 0.6 volts that were similar to the turn on values for O2 Tank 1, i.e. normal indications. Approximately three seconds later, the first of three anomalous voltage spikes occurred with an approximately 2 volt transient drop and a 11 amp current increase followed by a much larger spike 15 seconds later and another 3 seconds after that. Due to the nature of timing of telemetry received, it is possible that if a larger spike of less than 0.1 seconds duration had occurred it may have not been recorded - let alone been observable. It was concluded that low level combustion started with the first spike so it is reasonable to assume that turning the fan motors OFF at that particular point would not have stopped the subsequent failure of Tank 2. After the "bang" and C&W - MAIN B UNDERVOLT, Jack left the left hand seat and floated over to the right hand side and observed that Main B had normal voltages, normal amps and normal fuel cell flows and concluded that it was a transient spike that had generated the C&W and he asked Fred if he recalled the 80 amp spike that had occurred in training. Jack was therefore, more concerned with a LM hull beach and wanted to get the hatch closed. Fred reported to Mission Control that "the voltage is - is looking good" and also that he recalled MAIN B had indicated an amp spike on it once before however, by the time that Fred got into position, the instrumentation was no longer "normal." As I have discovered in my career, a rapid unexpected event is more difficult to resolve immediately than at some time subsequent to the event. |
oly Member Posts: 1294 From: Perth, Western Australia Registered: Apr 2015
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posted 10-04-2021 11:40 PM
quote: Originally posted by Paul78zephyr: The problem was not simply that the O2 tanks had been built with inadequately rated thermostats...
The tanks were not built with "inadequately rated thermostats," NASA changed the voltage used in some electrical systems of the ground support equipment and spacecraft systems after the tank design had been finalised, which created a requirement to modify the fan, heater, and thermostat systems installed in the O2 tanks post-manufacture. The thermostat switch rated voltage and the procedure to use the tank heaters out of design parameters, causing high tank internal temperature, are considered to be the most probable cause.Once the tanks were installed in the service module, access to the internal components of the O2 tanks was not possible without the tank being removed, and the modification of the tank systems required that the tanks be returned to the contractor to have the work done. The tanks needed to be cut open to facilitate the modification and welded shut after the work was done. The O2 tanks were, I understand, manufactured by Beech, and there has always been some question over how the thermostat wiring modification was not completed during the time it was returned to the contractor. I do not know having if the tank returned with damage created a distraction for the repair venue or if the documentation never called ou for the thermostat system to be changed, or, it was just plain missed. The investigation board determined that the probability of the tank systems being damaged by the fall during the tank removal was minimal. The investigation into the tank damage was well documented and the decision to allow the tank to remain in service has been well covered. The problem of draining the tank contents and the workaround of using the tank heater to "boil off" the remaining oxygen, causing damage to the electrical wiring insulation, was a theory that was tested to confirm the scenario possibility. There was the previous tank stirs carried out during the Apollo 13 mission that did not result in an explosion, it was not the first time that the tank fans had been powered during the flight. The post-flight investigation never determined the exact cause of the failure, it produced a theory that was accepted by the board. There is a possibility that a pressure vessel simply failed at that exact moment, or that an unknown failure point was never identified. The program could not have moved forward without attributing the failure to a cause. Each heater is protected with a thermostatic switch, mounted on the heater tube, which is intended to open the heater circuit when it senses a temperature of 80° F. In tests conducted at MSC since the accident, however, it was found that the switches failed to open when the heaters were powered from a 65 V dc supply similar to the power used at KSC during the detanking sequence. Subsequent investigations have shown that the thermostatic switches used, while rated as satisfactory for the 28 V dc spacecraft power supply, could not open properly at 65 V dc. This quote from the investigation board's findings is very telling because it shows that the thermostat switch acceptance testing was not considered during the modification development and that it was during the board's investigation that the problem switch was determined. The investigation board also interviewed technicians and engineers involved in the use of the tank heaters to boil off the liquid oxygen. Many of the principals in the discussions were not aware of the extended heater operations. Those that did know the details of the procedure did not consider the possibility of damage due to excessive heat within the tank and therefore did not advise management officials of any possible consequences of the unusually long heater operations. |
David C Member Posts: 1299 From: Lausanne Registered: Apr 2012
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posted 10-05-2021 05:19 AM
quote: Originally posted by pterodactyl: "Apollo 8 would NOT have had that failure."
Pilots tell themselves, and each other this kind of thing all the time; and sometimes it’s even true. Seriously though, in a risky business it’s a normal defence mechanism that allows you to keep on going up. Oh and if it was Borman, remember that he absolutely didn’t suffer from space sickness on Apollo 8 until about 40 years later when you know maybe, perhaps he did. That wrong-footed more than one of his colleagues who were still towing the absolutely no-way party line. |
Henry Heatherbank Member Posts: 290 From: Adelaide, South Australia Registered: Apr 2005
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posted 10-05-2021 07:12 AM
Not to get too far off topic, but Borman's denial/suppression of SAS also had consequences for people like Rusty Schweickart whose career in rotation was sidelined after he became the guinea pig for tests after his Apollo 9 episode. Lost his chance to fly a later Apollo, in my view, possibly as Dave Scott's LMP on 15. |
Jim Behling Member Posts: 1683 From: Cape Canaveral, FL Registered: Mar 2010
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posted 10-05-2021 12:08 PM
quote: Originally posted by pterodactyl: ...and seen the short circuit when the heater switch was actuated.
They would not have known that there was a short. |
taneal1 Member Posts: 271 From: Orlando, FL Registered: Feb 2004
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posted 10-07-2021 08:39 PM
quote: Originally posted by Andy Anderson: I wonder what was said that implied the Apollo 8 crew would have been closely monitoring the "voltmeter" during a cryo stir or how they believed the cryo stir should have been carried out.
Excellent post Andy! I have the same documentation on Apollo 13 that you have presented, but not the procedures for Apollo 8. *IF* the procedure for Apollo 8 included monitoring the amp load during *every* cryo stir, then Borman's or Anders' statement is not unreasonable. However, it is far from certain that the spike actually appeared on the CSM ammeter, and that it was high enough/long enough to warrant aborting the cryo-stir. Another factor: this was only the second flight of the CSM, and it was a day or more away from Earth when in this scenario, the stir occurred. They may have been more cautious than later flights and monitored the ammeter. The Apollo 13 crew had four flights (three to the moon and back) with no fuel cell issues. How dangerous was a cryo-stir considered to be, anyway? It doesn't sound like anyone was concerned re this procedure. |
oly Member Posts: 1294 From: Perth, Western Australia Registered: Apr 2015
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posted 10-07-2021 11:48 PM
Prior to the spike, how do the indication for the doomed cryo stir compare the the previous ones done on this flight? |
Jim Behling Member Posts: 1683 From: Cape Canaveral, FL Registered: Mar 2010
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posted 10-11-2021 01:53 PM
The gauges were likely too slow to show a spike in amps. |